We released the infraspinatus tendons of six sheep, allowed retraction of the musculotendinous unit over a period of 40 weeks and then performed a repair. We studied retraction of the musculotendinous unit 35 weeks later using CT, MRI and macroscopic dissection. The tendon was retracted by a mean of 4.7 cm (3.8 to 5.1) 40 weeks after release and remained at a mean of 4.2 cm (3.3 to 4.7) 35 weeks after the repair. Retraction of the muscle was only a mean of 2.7 cm (2.0 to 3.3) and 1.7 cm (1.1 to 2.2) respectively at these two points. Thus, the musculotendinous junction had shifted distally by a mean of 2.5 cm (2.0 to 2.8) relative to the tendon. Sheep muscle showed an ability to compensate for approximately 60% of the tendon retraction in a hitherto unknown fashion. Such retraction may not be a quantitatively reliable indicator of retraction of the muscle and may overestimate the need for elongation of the musculotendinous unit during repair.
Fixation of the glenoid component is critical to the outcome of total shoulder arthroplasty. In an in vitro study, we analysed the effect of surface design and thickness of the cement mantle on the pull-out strength of the polyethylene pegs which are considered essential for fixation of cemented glenoid components. The macrostructure and surface of the pegs and the thickness of the cement mantle were studied in human glenoid bone. The lowest pull-out forces, 20 ± 5 N, were for cylindrical pegs with a smooth surface fixed in the glenoid with a thin cement mantle. The highest values, 425 ± 7 N, were for threaded pegs fixed with a thicker cement mantle. Increasing the diameter of the hole into which the peg is inserted from 5.2 to 6.2 mm thereby increasing the thickness of the cement mantle, improved the mean pull-out force for the pegs tested.
In this prospective, randomised study, we have compared the wear rate of cemented, acetabular polyethylene cups articulating with either a 22 mm or a 32 mm cobalt-chromium head. We evaluated 89 patients who had a total of 484 radiographs. The mean follow-up period was 71.4 months (SD 29.1). All the radiographs were digitised and electronically measured. The linear wear rate was significantly higher during the first two years and decreased after this period to a constant value. We suggest that this is partly due to a ‘run-in’ process caused by irregularities between surfaces of the cup and head and an initial plastic deformation of the polyethylene. The mean volumetric wear was 120.3 mm3/year for the 32 mm head, which was significantly higher than the 41.5 mm3/year for the 22 mm heads. The mean linear wear rate was not significantly different. We were, however, unable to find radiological signs of osteolysis in the patients who had higher wear rates.