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Orthopaedic Proceedings
Vol. 99-B, Issue SUPP_8 | Pages 5 - 5
1 Apr 2017
Alshuhri A Miles A Cunningham J
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Introduction

Aseptic loosening of the acetabular cup in total hip replacement (THR) remains a major problem. Current diagnostic imaging techniques are ineffective at detecting early loosening, especially for the acetabular component. The aim of this preliminary study was to assess the viability of using a vibration analysis technique to accurately detect acetabular component loosening.

Methods

A simplified acetabular model was constructed using a Sawbones foam block into which an acetabular cup was fitted. Different levels of loosening were simulated by the interposition of thin layer of silicon between the acetabular component and the Sawbones block. This included a simulation of a secure (stable) fixation and various combinations of cup zone loosening. A constant amplitude sinusoidal excitation with a sweep range of 100–1500 Hz was used. Output vibration from the model was measured using an accelerometer and an ultrasound probe. Loosening was determined from output signal features such as the number and relative strength of the observed harmonic frequencies.


Orthopaedic Proceedings
Vol. 94-B, Issue SUPP_XXXVI | Pages 59 - 59
1 Aug 2012
Bone M Cunningham J Field J Joyce T
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Finger arthroplasty lacks the success seen with hip and knee joint replacements. The Van Straten Leuwen Poeschmann Metal (LPM) prosthesis was intended for the proximal interphalangeal (PIP) joints. However revision rates of 30% after 19 months were reported alongside massive osteolysis. Three failed LPM titanium niobium (TiNb) coated cobalt chrome (CoCr) components were obtained- two distal and one proximal.

All three components were analysed using an environmental scanning electron microscope (ESEM). This gave the chemical composition of the surface to determine if the TiNb surface coating was still intact. The distal components were analysed using a ZYGO non-contact profilometer (1nm resolution) with the proximal component unable to be analysed due to its shape. ZYGO analysis gave the roughness average (Ra) of the surface and determined the presence of scratches, pitting and other damage.

Images obtained from both the ZYGO and the ESEM indicated that the surfaces of all components were heavily worn. On the articulating surfaces of both distal components unidirectional scratching was dominant, while the non-articulating surface showed multidirectional scratching. The presence of unidirectional scratching suggested two-body wear, whilst the multidirectional scratching on the non-articulating surface of the distal component suggested that trapped debris may have caused three-body wear.

The ESEM chemical analysis showed that in some regions on the distal component the TiNb coating had been removed completely and in other areas it had been scratched or penetrated. On the proximal component the TiNb coating had been almost completely removed from the articulating surfaces and was only present in small amounts on the non-articulating surfaces. There was little evidence of bone attachment to the titanium coating which was intended to help provide fixation.

ESEM images showed the coating had been removed in some sections where there was minimal scratching, suggesting this scratching did not impact significantly in the coating removal. Therefore here the main cause of coating removal may have been corrosion, although scratching may have also have played a part.

The osteolysis reported clinically may have been linked to the wear debris from the failed coating.