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Orthopaedic Proceedings
Vol. 93-B, Issue SUPP_III | Pages 298 - 298
1 Jul 2011
Langton D Jameson S Joyce T Ramasetty N Natu S Antoni N
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In our independent centre, from 2002 to 2009, 155 BHRs (mean F/U 60 months) have been implanted as well as 420 ASR resurfacings and 75 THRs using ASR XL heads on SROM stems (mean F/U 35)

During this period we have experienced a number of failures with patients complaining of worsening groin pain at varying lengths of time post operatively. Aspiration of the hip joints yielded a large sterile effusion on each occasion. At revision, there were copious amounts of green grey fluid with varying degrees of necrosis. There were 17 failures of this nature in patients with ASR implants (12 females) and 0 in the BHR group. This amounts to a failure of 3.5% in the ASR group.

Tissue specimens from revision surgery showed varying degrees of “ALVAL” as well as consistently high numbers of histiocytes. Particulate metal debris was also a common finding.

The mean femoral size and acetabular anteversion and inclination angles of the ARMeD group/all asymptomatic patients was 45/49mm (p< 0.001), 27/20°(p< 0.001) and 53/48°(p< 0.08). Median blood chromium(Cr) and cobalt(Co) was 29 and 69 μg/L respectively in the ARMeD group versus 3.9 and 2.7 μg/L in the asymptomatic patients (n=160 with ion levels). Explant analysis confirmed greater rates of wear than expected.

Lymphocyte proliferation studies involving ARMeD patients showed no hyper reactivity to Cr and Co in vitro implying that these adverse clinical developments are mediated by a toxic reaction or a localised immune response.

Our overall results suggest that the reduced arc of cover of the fourth generation ASR cup has led to an increased failure rate secondary to the increased generation of metal debris. This failure rate is 7% in ASR devices with femoral components _47mm.